• The Roadster Factory Recovery Fund - Friends, as you may have heard, The Roadster Factory, a respected British Car Parts business in PA, suffered a total loss in a fire on Christmas Day. Read about it, discuss or ask questions >> HERE. The Triumph Register of America is sponsoring a fund raiser to help TRF get back on their feet. If you can help, vist >> their GoFundMe page.
  • Hey there Guest!
    If you enjoy BCF and find our forum a useful resource, if you appreciate not having ads pop up all over the place and you want to ensure we can stay online - Please consider supporting with an "optional" low-cost annual subscription.
    **Upgrade Now**
    (PS: Subscribers don't see this UGLY banner)
Tips
Tips

General TR Well that was close!

tinman58

Jedi Knight
Silver
Country flag
Offline
I went out for a drive to the grocery store in the TR3. All was going well until the motor seized. I rolled to a stop, and of course tried to start it up. Very slow cranking, played with a few things to no avail. I thought a valve broke, pulled the cover off and all was good. Just for fun I was going to try starting it once more before calling for help. To my surprise it fired up! Made a quick u-turn and headed for home. 1/2 mile later Bam same thing, this time I could smell the belt burning, coasted to a stop. Water pump? Alternator? Turns out the bolt holding the air cleaner came loose and went thru the carb and into the supercharger! Thinking the worst I pulled the belt loose and made it up the last hill and coasted home. After dinner I pulled off the s/c and found the bolt. So I tore the s/c apart and removed all the bits and pieces, filed down all the ruff edges and. Put it back together. I crossed my fingers and it fired right up. Went for a drive and everything seems fine. I think I got very lucky nothing major happened. E2EC09E7-E118-4B09-A7FB-BCFF1A6BFE3E.jpg
 

Gliderman8

Great Pumpkin
Country flag
Offline
Glad all is well... you got lucky!
 

Sarastro

Obi Wan
Silver
Country flag
Offline
At the risk of telling you something that you now already know, it's always a good idea to keep small hardware out of the inside of the air filter. I have a rule that I never allow anything inside the air filter that could fit down the bore of the carburetor. That means, especially, screws or nuts that could come loose.

As an example--below is a picture of the breather connection to the Weber carbs on one of my other cars. The elbow is actually a PVC pipe elbow, and the "screw" attaching it, on the inside, is made out of a piece of PVC adapter. It's far too big to fit down the bore of the carburetor. As simple as it seems in hindsight, I put a fair amount of thought into figuring out how I wanted to do this.

crankcaseventilation.jpg
 

Gliderman8

Great Pumpkin
Country flag
Offline
At the risk of telling you something that you now already know, it's always a good idea to keep small hardware out of the inside of the air filter. I have a rule that I never allow anything inside the air filter that could fit down the bore of the carburetor. That means, especially, screws or nuts that could come loose.
I bought a TR6 a few years ago and heard this strange noise after I got it started. It sat many years in the sellers garage.
When I pulled the head I found this lock washer sitting on top of #3 piston.
56D1C56D-EC2B-42D7-B9DB-9529DD2F1EE8.jpg
 

Sarastro

Obi Wan
Silver
Country flag
Offline
Wow! Good catch!

You're lucky it didn't do more damage--I suspect a lot of people would have just driven it and hoped the noise would go away.
 

Gliderman8

Great Pumpkin
Country flag
Offline
Wow! Good catch!

You're lucky it didn't do more damage--I suspect a lot of people would have just driven it and hoped the noise would go away.
Thank goodness there was no damage. It was a weird "pinging" sound. The guy I bought the car from never worked on his car and always took it to his "mechanic".
His mechanic probably dropped it and it went into the intake and never said anything to the owner. My eyes almost popped out of my head when I saw the lock washer sitting on top of the piston.
 

Gliderman8

Great Pumpkin
Country flag
Offline
Thumbs up for the cast iron head!
You can say that again! Luckily the walls of the cylinder were fine the only damage was the intake valve was leaking (no surprise there). I have the damaged head in my garage and plan on getting it repaired with hardened exhaust valve seats.
 
D

Deleted member 8987

Guest
Guest
Offline
I had a brain-damaged Army vet working for me (encephalitis) who was a motor pool mechanic.

So...we get a GM diseasemal pickup in, he's got the air cleaner off doing something.
In the doorway of the shop...exhaust at the open window to the boss' office.

He laid a red shop rag on top of the inlet to keep from dropping anything in.

Gets done and starts it.
Yup.
Forgot the rag.

Pink fog FILLED the office.
Didn't seem to have hurt anything, ran fine (well, as good as those converted gasoline engines ran).
 

Alfred E. Neuman

Jedi Trainee
Country flag
Offline
I had a brain-damaged Army vet working for me (encephalitis) who was a motor pool mechanic.

So...we get a GM diseasemal pickup in, he's got the air cleaner off doing something.
In the doorway of the shop...exhaust at the open window to the boss' office.

He laid a red shop rag on top of the inlet to keep from dropping anything in.

Gets done and starts it.
Yup.
Forgot the rag.

Pink fog FILLED the office.
Didn't seem to have hurt anything, ran fine (well, as good as those converted gasoline engines ran).
Tech got finished with an intake manifold cleaning/oil cooler replacement on a Mercedes 642 Diesel at the shop. Got it all back together and started it, wouldn't catch for a minute. Nothing to worry about yet since it takes a bit for the fuel rail to get pressure after it's been off. Finally got it to cough to life and it was stumbling all over itself. BROWN smoke out the tailpipe.
Yep, left the blue paper shop towels in the intake ports and they got pulled through the cylinders, chewed up, and spit out onto the CATs.
Off comes the manifold again to check for bent valves - none. Cleaned everything as well as possible, put it back together, and it coughed to life again.
A few trips around the block and the CATS finally burned off the remnants of the paper towels in what looked like a Saturn V rocket taking off. :smile:
 

bnw

Jedi Warrior
Country flag
Offline
With the carb removed, I was tightening the two large Philip's headed screws under the carb that hold the 1BBL Carter carb body together on the Chrysler 225 slant 6. A very common problem on the 225. Put it back together, started it up, and WHAM! BANG BANG BANG just like a rod let loose. I had no idea what had happened. It was quitting time and as I was cleaning up my bench, I saw my favorite magnetic tip screwdriver missing the replaceable Phillip's bit. So I pulled that huge cast iron head the next day and found my bit standing straight up where it was pounded into the #5 piston crown. There were 7 nicks on the crown surrounding the bit. So I figured the bit stayed in the screw head when I put the carb back on the intake. It banged around for 7 revolutions before it got caught in an upright position where it proceeded to get pounded into the piston crown by hitting the head. I kept that piston with the bit in place for 25 years. Sadly, it disappeared during one of my moves.
 
Similar threads
Thread starter Title Forum Replies Date
tinman58 That was close! Triumph 10
Stewart That was to close MG 2
AngliaGT "I WAS SEVENTH!" Racing 0
mezy Look what I was in yesterday Other Cars 14
S TR2/3/3A My tr3 was stuck in reverse after a short drive Triumph 3
S TR2/3/3A my OD stopped working after it was working Triumph 25
dougie Use your car as it was meant to be used Austin Healey 15
drooartz General MG Surprisingly enough, I was right! MG 7
JPSmit well that was fun Spridgets 1
P TR6 What make and size tire was on the TR6 when it left the factory? Triumph 7
S TR2/3/3A TR3 has me stumped, it runs then dies over and over and the exhaust system was pulled Triumph 9
Gliderman8 General MG The car that never was MG 6
Got_All_4 TR6 This frame was sectioned Triumph 9
S TR2/3/3A and the radiator was leaking. Triumph 7
Jim_Gruber Boy was I ever surprised on Saturday Spridgets 11
K TR2/3/3A It was all going so well....... Triumph 11
T Was Sophia Loren ever photographed with a Healey? Austin Healey 2
Trevor Jessie When was the last time you bled your brakes? Spridgets 4
Jim_Gruber Hubs a Rocking on side where Speedi Sleeve was installed Spridgets 5
HealeyRick DMH was a Nasty Boy Austin Healey 2
catfood So thats what it was... Other British Cars 0
Zitch TR4/4A Door Weather Strip Channel - Was this added? Triumph 4
tinman58 General TR It was just a loose wire Triumph 15
Jim_Gruber I woke up Bugsy this afternoon after about a month long nap and he was cranky Spridgets 7
T Was the Bugeye a Mk I from the get-go? Spridgets 9
PC Dang, that was too good to be true... Restoration & Tools 3
Jim_Gruber Bugsy was out for his first real romp today! And it was fun!!!! Spridgets 3
JPSmit Tesla - but that's not what was interesting Other Cars 2
H At least the Bugeye Shirt was at the HPDE this weekend. Spridgets 5
drooartz MGB Today was a good day - the MGB is legal! MG 6
longbridgehealey When did you buy your first LBC, and what was it? Spridgets 46
S What was it? Other Cars 18
J Cloth interior in AH-3000? Was it ever fitted? Pleated inserts maybe? Austin Healey 7
Sopwith_Camel was this wire brown in 1967? Jaguar 5
GTP1960 TR2/3/3A It was running great....until Triumph 17
CZ_Dave MGB Was I missed? MG 2
bighealeysource Was 100M from Chasing Classic Cars sold this weekend? Austin Healey 20
S TR2/3/3A 37XXX and 27XXX the steering column was split Triumph 6
C The 1956 Jaguar XKSS was one of a kind Jaguar 10
H Aston Martin DB4 converible found in UK awhile back--what was paid for it? Other British Cars 0
C Was the 2013 Jaguar XJ Ultimate the Crown Jewel of Luxury? Jaguar 0
C Just how good was the Jaguar E-Type? Jaguar 10
JPSmit What was on the trailers was most interesting today Spotted 2
DanLewis And I thought the Bugeye was small... Spridgets 6
jaegzie Disc brake upgrade was fine now major alignment issue. Spridgets 6
S What Was it Like? Spridgets 10
krswen Remember when carb cleaner was so strong .... Restoration & Tools 12
HealeyRick Wedge It Was All the TR7's Fault Triumph 7
DNK Was this real to start? Lotus 7
RickB I was wrong. Again. Not ignition switch! Spridgets 16

Similar threads

Top