Years ago Randell help with a similar problem. Someone had taken the spring out and stretched the spring to help put pressure on the cork washers, probably to stop a leak. What happen was the spring was too long now and the jet assembly would not return, leaving about 1/16 to the base return. The stretched spring would hold the jet out when the choke was pulled. I could push the jet back with my finger, so at this time I had no idea the problem was the spring. I figured the jet was sticky. However, this let too much fuel run into #1 and foul the plug, and hardly effected number 2.
Anyways, I found a stock spring that was about 3/8 to a 1/4 shorter and that fixed. I latter bought some springs from Joe in NY and those springs where correct. To me it sounds like they fixed your car by adding shims in the assembly to apply more pressure to the glad washers to stop a leak.
Steve
Anyways, I found a stock spring that was about 3/8 to a 1/4 shorter and that fixed. I latter bought some springs from Joe in NY and those springs where correct. To me it sounds like they fixed your car by adding shims in the assembly to apply more pressure to the glad washers to stop a leak.
Steve