That's interesting...reminds me of an old accident we studied in aircraft accident investigation school.
An F84 was being flown by a brand new pilot when the front wheel cocked 90 degrees after take off. Normally, an experienced pilot would fly the jet right back to the runway, since the problem was normally a broken centering spring...and once the wheel touched back down it would center itself. BUT, occasionally the wheel would not center, so the pilot would have to stop the jet with no front wheel steering control, at the risk of rolling the plane over on it's back.
This was in the 1960's, and the F84 was already way obsolete by then...so the decision was made that the plane was worth less than the cost of a pilot, so they decided to fly the plane to a controlled ejection sight and let the rookie shut it down and then bail out, using the nylon (parachute) let down. Well, since he had just taken off and had plenty of gas, they took over 30 minutes, making sure he removed all his loose gear, stowed anything else, and fully went through all the checklists. He then popped the canopy...not off, but open. For some unknown reason the F84 canopy was made to raise in flight, but it would not pop off until AFTER the ejection handles were pulled. So, rookie pulled the handles for the ejection.
What happened is the rookie's seat started up the rails, but the canopy explosive squibs never fired. Had it been closed, the seat would have punched right through the plexiglass, but, being open, the rookies head went right through the front canopy metal rail...knocking him unconscious. Since the F84 used a first generation ejection seat, there was no automatic deployment of his chute, so he...and the seat...rode it into the desert together. Of course he died.
I know...what's this got to do with Bobby's weak connection?!? Well, in the investigation it was found that more than a decade prior, during manufacture of the plane, some line worker had installed the connector for the canopy squibs using 2 male connectors. So, the male prongs touched each other, and for every monthly test for over a decade, the connector showed that it passed excellent voltage through it. It checked good during hundreds of tests. But, when the high amperage passed through the mis-fit connector when it was really needed to save a Pilot's life, it could not transfer enough juice to fire the explosive canopy squibs!
The school used this sad case to show how every accident is a chain of events...all of which have to align perfectly for an accident to happen. In this case...a designer designed a connector that would allow a male to male to fit together...it was then actually mis-fit together, only once in the entire F84 production (they inspected all planes after the incident to know)...a chance spring failure on the nose wheel occurred during a flight with a rookie pilot....the decision was made to open the canopy before the ejection...and, well, it cost a rookie his life.
Oh...what happened to the plane after the ejection? Well, it was trimmed so well that it glided right down and made a perfect landing on its own. The pilot would have survived the dead stick landing just fine. It was not that particular rookie's day.